BMB Munai Announces Production Increase at Kariman-1 Well
OREANDA-NEWS. November 23, 2010. BMB Munai, Inc. (NYSE Amex: KAZ) announced initial production rates from its Kariman-1 well following completion of a sidetrack well bore commenced in August 2010. "The well has produced at the stable rate of 925 bpd during the past 15 days," said Gamal Kulumbetov, Company CEO, noting, "This significant increase in production has been achieved at a cost of only USD 1.7 million dollars and was completed in less than four months."
The Kariman-1 well was originally drilled by the State in 1967 targeting Jurassic formations at a depth of
In August 2010, the Company started a sidetrack well, targeting middle Triassic layers. The sidetrack well was drilled by a subcontractor, Xibu Drilling to a depth of
BMB Munai is an independent oil and gas company engaged in the exploration and test production of crude oil and natural gas in
The information contained in this release includes forward -looking statements that are subject to risks and uncertainties that could cause actual results to differ materially. Certain statements contained herein constitute forward -looking statements within the meaning of the Private Securities Litigation Reform Act of 1995. Such forward -looking statements involve known and unknown risks, uncertainties and other factors, which may cause the actual results, performance or achievements of the Company to be materially different from those expressed or implied. Forward -looking statements involve risks and uncertainties, including but not limited to, risks described in the Company's periodic reports on file with the Securities and Exchange Commission.
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